Reduction in Failure of Slag & Metal Ladle Auto Couplings

B. D. Babu & DPS Brar

Blast Furnaces, Bhilai Steel Plant,

Steel Authourity of india Ltd, Bhilai. 490001

e-mail:

ABSTRACT

Bhilai Steel Plant, Pioneer unit of Steel Authority of India Limited (SAIL), a Maharatna Company in the field of Iron & Steel, is India's sole producer of Rails, 260 Mtr Long Rails & Heavy Steel Plates and also specializes in other products ie, Wire Rods and Merchant products. BSP is accredited with ISO 9001:2000 Quality Management System Standard and all Saleable products of Bhilai Steel Plant come under the ISO umbrella.

Blast Furnace produces Hot Metal, which is transported as Rake of 3-4 Ladles in shortest possible time to Steel Melting Shops so that minimum heat is lost & increase in availability of ladles for Hot Metal Circuit. These Rakes are formed by joining Hot Metal ladle bogies with the help of Auto Couplers. Out of 232 Auto couplers installed in locos & bogies, there were approximately 100 failures every year. Frequent Failure of these Auto Couplers was the major problems faced by Blast Furnace, as failure leads to delay in Hot Metal Disposal, Heat Loss, Bunching of rakes, and reduction in Hot Metal/Slag Ladle availability. Reduction in Ladle availability for tapping results in holding furnace under low blast/Low production state. This directly effects the Blast furnace productivity.

This Project was undertaken to identify and eliminate the problem arising breakdowns. On data analysis of Auto Coupler failures, it was found that failure of Couplers was mainly on Shank & Wedge area. Team studied the problem and recommended modifications in material & Design of Shank & Wedge. The modifications had resulted in “Zero Failure in Modified Auto couplers installed since Apr’2009” leading to tangible savings of Rs.51.59 Lakhs per annum and intangible benefit of Rs.3.0 Crores due to reduction of Low Blast duration by 41.75 Hrs. This has also resulted in Safe Working with minimum maintenance staff.

INTRODUCTION

Bhilai Steel Plant, the NINE times winner of Prime minister trophy, is the flagship unit of Steel Authority of India limited (SAIL).It is an integrated steel plant producing steels for general construction as well as special steels catering mainly to the needs of Engineering, Power, Railways, Automotive & Defense sectors. This is the first Steel Plant in India to cross 5MT mark. As symbol; of a “New Age” in India, Bhilai Steel Plant has been consistently performing despite several odds and generating profits for the last twenty two years.

Historically, Bhilai Steel Plant has been into value engineering since 1972, but it got the momentum through its Value Engineering program in 2008 One of the successful projects is the subject of the present case study which was done in Blast Furnace and implemented in Apr’2009.

Blast Furnace is the mother of an integrated steel plant. Bhilai Steel Plant is the flagship unit with production capacity of 5.3 MT by 7 Blast Furnace. Hot metal tapped in Ladles and is supplied to Steel Melting Shop – I & II, Foundry and Pig Casting Machine.The slag produced is sent to slag granulation Plant & Slag Dump through Slag Thimbles. Total 89 Hot Metal Ladles and 45 Slag Thimbles are in circulation. All these Ladles are joined together with the help of two Auto Couplers (One at each side). The process layout of Blast Furnace is as shown in figure below:

ABOUT AUTO COUPLER

Auto Coupler is a device used for joining two ladle cars. It works under the action of impact of collision between two ladle cars (Shown in Fig below & next page). The couplers get engaged and locked automatically. The operation of an external handle disengages the same.

A pair of Auto Couplers, in engaged condition, ensures the joint of two adjacent ladle cars. They transmit the force of pull by which the whole train of ladle car moves on Rail tracks. It works to transfer the ladle car from one place to another without detaching of any of the ladle cars in the train during movement. The various internal components make the systemto get engaged with the other coupler on slight impact. It is automatically responsible for the transmission of the pulling and pushing load, which moves the train of ladle cars to & fro from Blast Furnace area to Various Customer Destination.

PROBLEM:

During train formation & movement, frequent breakdown in Auto coupler were observed. These breakdowns resulted in delay in train movement, restricted traffic, increased cycle time in Hot Metal & Slag Ladle Circuit, Low blast to Blast Furnace and Production & Heat/Energy loss.

Approach & Methodology

A cross- functional team constitutes of members from Operation, Mechanical, VE trained persons from industrial Engineering. The team was given the task of coming up with a Value Engineering proposal for a new cost effective solution for failure of Auto Coupler.

Information Phase:

To study & understand the design, function and problematic area of Auto Coupler, detailed sketch (given below) was thoroughly studied. Keeping in view all the aspects of function, design, material, operations etc each part & Sub-parts were discussed and noted for further analysis.

EXISTING AUTO COUPLER

TOP VIEWSIDE VIEW

OBSERVATIONS & FINDINGS

Data analysis for Breakdown pattern, Design and material of Auto Coupler was carried out in detail. All aspects of problem were studied and discussed with concerned official to reach at the conclusion that Shank & Wedge area of Auto Coupler are the parts of failure in this coupling.

S. No / Month / No of Breakdown / Delay in mins.
1 / April / 8 / 3.93
2 / May / 11 / 5.4
3 / June / 6 / 2.95
4 / July / 9 / 4.42
5 / August / 6 / 2.95
6 / September / 12 / 5.9
7 / October / 9 / 4.42
8 / November / 7 / 3.44
9 / December / 10 / 4.91
10 / January / 9 / 4.42
11 / February / 8 / 3.93
12 / March / 11 / 5.4
Total / 106 / 52.07

Function Phase:

Function analysis of Auto Coupler was elaborated and identified to describe Higher Order Function, Lower Order Function, One Time Function and All time function. these are displayed as under:

HIGHER ORDER FUNCTION / LOWER ORDER FUNCTION
Facilitate Train Movement / Use Shank
ONE TIME FUNCTION / ALL TIME FUNCTION
Transfer Load, Withstand Impact, Bending, Shear & Shock / Connect Parts, Hold Parts

The functional analysis of Shank in Auto Coupler is displayed as under:

FUNCTION / BASIC /
VERB / NOUN / SECONDARY
Transfer / Load / Basic
Withstand / Impact / Secondary
Withstand / Shear / Secondary
Withstand / Tension / Secondary
Withstand / Shock / Secondary
Prevent / Bending / Secondary
Connect / Parts / Secondary
Hold / Parts / Secondary
Facilitates / Fixing / Secondary
Increase / Weight / Secondary
Increase / Replacement / Secondary

The functional analysis of Wedge in Auto Coupler is displayed as under:

FUNCTION / BASIC /
SECONDARY
VERB / NOUN
Facilitates / Locking / Basic
Facilitates / Horizontal Movement / Secondary
Withstand / Shock / Impact / Secondary
Withstand / Shear / Secondary
Withstand / Tension / Secondary
Facilitates / Maintenance / Secondary
Facilitates / Fixing / Secondary
Withstand / Wear / Secondary
Prevent / Bending / Secondary

Function-Cost –Worth Analysis

Function Cost –Worth Analysis was carried out by comparing the Cost of Shank & Wedge separately with respect to worth taking Manual Coupling Cost as basis of Worth. The value gap & Value Index was thus evaluated as below:

S. No / Items / Existing Cost (C) / Worth (W) / Basis of Worth / Value gap
(C-W) / Value Index (C/W)
1 / Shank / 20500 / 10250 / Manual Coupling Cost / 10250 / 2
2 / Wedge / 890 / 665 / 225 / 1.33

CREATIVITY PHASE

In the creativity phase, the Team generated 07 ideas by brainstorming during the workshop,out of which 4 ideas were for Shank and 3 ideas were for Wedge. One idea each for Shank & Wedgewere selected due to their outperformance in feasibility ranking matrix.

Ideas generated for Shank:

  1. Change in material composition to provide adequate Strength (IS:2708 GrII).
  2. Improve Design by altering Shape and Size ie, Increase thickness from 20 mm to 25mm.
  3. Improve alignment by installing Support Springs on both sides.
  4. Avoid Malfunction / Mal-operation by educating Porter & Driver.

Ideas generated for Wedge

  1. Replace Wedge arrangement by Heat Treated Cylindrical Pin Arrangement.
  2. Avoid additional support plate at the Impact area (Si-Mn Spring Steel).
  3. Provide greasing at the contact points of Cylindrical Pin.

EVALUATION PHASE

IDENTITY
A / B / C / D / E / F / G / H / I / SCORE
COST / QUALITY / TIME / SAFETY / FEASIBILITY / RELAIBI-LITY / EASE OF OPERATION / MAINTAIN-ABILITY / WEIGHT
A / B 3 / C 2 / D 3 / E 2 / F 3 / G 2 / H 1 / A 1 / 2
3 points for
Major
Difference
2 points for
Medium
Difference / B / B 3 / D 3 / B 2 / B 2 / G 2 / B 1 / B 2 / 14
1 point for
Minor
Difference
No points for
No Difference / C / D 3 / E 2 / F 2 / G 1 / C 2 / C 1 / 6
D / D 2 / D 0 / D 2 / D 3 / D 2 / 19
E / F 2 / G 2 / H 1 / E 1 / 6
F / F 2 / F 2 / F 1 / 13
G / G 2 / G 2 / 12
H / H 1 / 4
I / 1

DECISION MATRIX

Based upon the evaluation phase, ideas were further evaluated based on decision matrix for wedge & Shank of Auto Coupling.

Detail of Decision Matrix for Shank is as given below:

CRITE RIA


IDEAS / COST / QUALITY / TIME / SAFETY / FEASIB-ILITY / RELAIB-ILITY / EASE OF OPERATION / MAINTAIN-ABILITY / WEIGHT / TOTAL POINTS / RANKING
Weightage / A X 2 / B X 14 / C X 6 / D X 19 / E X 6 / F X 13 / G X 12 / H X 4 / 1 X 1
Material Strengthening / 1 / 4 / 1 / 4 / 3 / 4 / 2 / 2 / 4 / 250 / I
2 / 56 / 6 / 76 / 18 / 52 / 24 / 12 / 4
Improve Design / 1 / 3 / 1 / 3 / 3 / 3 / 2 / 3 / 2 / 202 / III
2 / 42 / 6 / 57 / 18 / 39 / 24 / 12 / 2
Improve Alignment / 2 / 2 / 2 / 2 / 1 / 1 / 1 / 1 / 2 / 119 / IV
4 / 28 / 12 / 38 / 6 / 13 / 12 / 4 / 2
Avoid Mal-operation / 4 / 3 / 3 / 3 / 4 / 3 / 4 / 3 / 1 / 249 / II
8 / 42 / 18 / 57 / 24 / 39 / 48 / 12 / 1

Detail of Decision Matrix for Wedge is as given below:

CRITE RIA


IDEAS / COST / QUALITY / TIME / SAFETY / FEASIBILITY / RELAIBILITY / EASE OF OPERATION / MAINTAINABILITY / WEIGHT / TOTAL POINTS / RANKING
Weightage / A X 2 / B X 14 / C X 6 / D X 19 / E X 6 / F X 13 / G X 12 / H X 4 / 1 X 1
Heat Treated Cylindrical Pin / 4 / 4 / 2 / 4 / 3 / 4 / 4 / 4 / 2 / 288 / I
8 / 56 / 12 / 76 / 18 / 52 / 48 / 16 / 2
Additional Support Plates / 2 / 3 / 2 / 3 / 2 / 3 / 2 / 3 / 2 / 204 / III
4 / 42 / 12 / 57 / 12 / 39 / 24 / 12 / 2
Provide Lubrication / 2 / 3 / 2 / 3 / 3 / 4 / 4 / 3 / 1 / 246 / II
4 / 42 / 12 / 57 / 18 / 52 / 48 / 12 / 1

RECOMMENDATIONS

It was decided to take up the top ranking proposals of Shank & Wedge respectively for implementation. The proposals for implementation For Shankis to change the specification (From M:201 Gr B to IS:2708 Grill )of Auto Coupler to avoid Mal-operation and forWedgeInstalling heat treated Cylindrical Pin for fixing coupler.

IMPLEMENTATION / SUPPORTING DATA SHEET

PLAN FOR SHANK

RECCOMENDATIONS / ACTION / RESPONSIBILITY / COMPLETION DATE
Change in Material Specification of Auto Coupler from M:201 Gr.B to IS:2708 Gr. II / Incorporate Material Specification in drawing / MB Sarkar & BD Babu / 31-01-2009
Issue enquiry to supplier / 30-04-2009
Receive Quotation / 15-06-2009
Evaluate Quotation / MB Sarkar BD Babu
TDN Naidu
V Mathai
DPS Brar / 30-06-2009
Place Order / 31-07-2009
Procurement / 31-12-2009
Implementation / 15-01-2010

PLAN FOR WEDGE

Installing Heat Treated Cylindrical Pin for fixing Coupler / Discussions / MB Sarkar & BD Babu / 15-01-2009
Replacement of Work order with priority / 31-01-2009
Cylindrical Pin collection / 28-02-2009
Implementation / All Team Members / 10-03-2009

Modified auto coupler

TOP VIEWSIDE VIEW

BENEFITS

DIRECT BENEFIT CALCULATION

Installed Auto Couplings in BF’s= 274 Nos.

Auto Coupling replacement on Failure (2008-09)= 106 Nos.

Cost of Existing Auto Coupling= Rs. 29400/-

Projected Auto Coupling replacement (Apr’09 – Aug’11)= 256 Nos.

Expected Expenditure for Projected Replacement= Rs. 7532000/-

Cost of Modified Auto Coupling= Rs. 47158/-

Modified Auto Coupling replacement (Apr’09 – Aug’11)= 150 Nos.

Expenditure on Modified Auto Coupling= Rs. 7073700/-

Reduction in replacement of Auto Coupling= 106 Nos.

Saving due to reduction in replacement= Rs. 5000000/-

Mandays Saving for 106 replacements= 159 Mandays

Savings in Cost of Mandays @1000/-= Rs. 159000/-

TOTAL SAVINGS:51.59 Lakhs

INDIRECT BENEFIT CALCULATION

Reduction in Delay in Disposal of Hot Metal may be accorded against failure of auto coupling.

Auto coupling Failure 2008-09 = 106 Nos

Total Delay in Hot Metal Disposal(DDHM) 2008-09 = 173.55 Hrs

DDHM due to Coupling Failure= 52.07 Hrs

Auto coupling Failure 2009-10= 64 Nos

Total Delay in hot metal disposal(DDHM) 2009-10 = 180.80 Hrs

DDHM due to Coupling Failure= 31.44 Hrs

Auto coupling Failure 2010-11= 38 Nos

Total Delay in hot metal disposal(DDHM) 2009-10 = 180.80 Hrs

DDHM due to Coupling Failure= 19.24 Hrs

Considering 7 % Breakdown in Total Ladle Cars (274)= 20 Nos

Expected DDHM Duration= 10.24 Hrs

DDHM Duration before implementation= 52.07 Hrs

Average Saving in delay Hrs (Annual) = 41.83 Hrs

Delay Cost/Hr due to Low Blast/Stoppage = Rs. 6 Lakhs

Benefit (Cost of delay):2.51 Crores/Yr

POST IMPLEMENTATION BENEFIT ASSESMENT
Direct Savings Calculation
Total Auto Couplings / 274
Annual Auto coupling replacement pre-implementation / 106
Projected Auto Coupling replacement without modification / 345
Cost of Old design Auto Coupling / 29400
Cost of One Modified Auto Coupler / 47200
Modified Auto Coupling Installed / 170
Extra Cost for Modified Auto Couplings Installed / 3026000
Failure of Modified Auto Coupling / 1
Savings in No of Auto Couplers replacement / 344
Savings due to reduction in failure / 16236800
Net Savings due to reduction in Auto Coupler requirement / 13210800
Mandays Saved for 344 replacements @1.5 Mandays/replacement. / 516
Savings due to Mandays reduction for replacement (Contractual Highly Skilled Worker Wages @ Rs.350) / 180600
Total Savings / 13391400
Say Total Savings of Rs 1.34 Crores

aCHIEVEMENT:

“ZERO FAILURE” in all Modified Auto Couplings

since installation (Apr’2009 – Till Date)